The Olds Engine
By luck, a friend said he had a 50 Olds
engine in pieces in his garage! I knew it would have much more power than
the flathead. For a few bucks I bought the parts hoping they
were all there! A true basket case! It came with an
engine to the '41 Ford transmission adapter, a 3/8 inch thick plate with the
appropriate holes matching both pieces. My friends helped get the block in my basement.
The
pistons, rods, crank main caps, timing chain and all other parts (I hoped,)
were in a big wood peach basket! Before I spent time and money on the
Olds I wanted to be sure it wasn’t going to burn oil! I wasn’t going
to have a "smoker" again! (Picture at left is the only one I
have from that time. It is the Olds in the '41. Performance, not
appearance was my first goal!
The auto parts store I dealt
with also had a machine
shop. They sent someone over to measure the size, taper and roundness
of the cylinder walls. As I watched him make the measurements he said;
"it’s borderline, it may be OK! "Maybe and OK" were not what I wanted
to hear! However, I paid very little for the engine so why not have it
bored out! An article in Hot Rod said you could bore a ’50 Olds block
1/8 inches and use ’55 Olds pistons. Sounded good to me, it would then
have 324 cubic inches versus the 303 in the '50. That was more than
the 265 and the new 283 Chevy V8 that had just been introduced. In
addition, the Chevy engine was very new and couldn't find those in the junk
yard at a price I could afford. Their were no "crate engine" programs at the time and I didn't have the money
if their were!
Went over to
the auto parts house and said "bore it out 1/8 inches I don’t want an oil
burner." They refused, swore they would be in the water jacket. I said,
being a determined young man, "Hot Rod says you can do it!!" I didn’t know
about potential core shift etc at that time. They said; "Take all
responsibility for creating a hole and buy the pistons from
us and we’ll do it." The machine shop had never bored out anything more than a 1/16 inch
before so they charged extra. To bore them out it would be $5.00 a hole
is what I remember.
That was about the same price they charged for each new piston as I recall. A lot of money but I said go!
After boiling the block they installed new cam bearings. I bought a
'55 Olds cam from the Olds dealer. The magazines said that was the low cost approach rather than buy an expensive Isky cam.
It had higher lift and duration and retained the hydraulic lifters and non
adjustable rockers. The machine shop also ground
the crank and sold me a rebuild kit, new bearings, gaskets, rings etc.
My friend with the 50 Merc was going to
auto mechanic school and said he would do a valve job on my heads as part of
his classes. Took him a while to finish but when I got them back found
he had polished the chambers and ports. You could see yourself in the
chambers!! Don’t know how much good it did but it sure looked great!
I recall rebuilding the 4 barrel carb
that came in that fruit basket of parts! I did the wok on a
portable coffee table in the
sun parlor. Cleaned all the parts in the basement with gasoline and boy did it smell
up the house! Took a few days but got it all back together following the
instruction sheet that came with the rebuild kit!
I received a phone call from the machine shop
saying two of the rods were stretched and there was a problem with the
thrust
surface on the crankshaft! Fortunately my buddy with the Merc
had a set of 50 Olds rods and a crack. He donated them to the project! I gave
the extra eight rods to the machine shop and asked
them to pick the ones that matched best! They found a good eight
from the 16! His crack was also find for regrinding.
Must
admit it didn’t seam like a problem putting the engine together without a
manual. Today I won’t touch a part without first consulting the service
manual. Everything went together correctly and when I put the bottom end
together I used Plastigage and checked all clearances. I remember the
machine shop had to wait for the pistons so they could mic each and finish
hone the bores to match. They even understood the importance of close
tolerances in the '50's! I recall phoning Uncle Fred and asking him to
drop off a torque wrench on his way home from work. Hot Rod said it was a must. He said.
"that’s not
what you need; you just need a pry bar." Hot Rod couldn’t be wrong and I
wanted this engine to be right. He came over the house with both. He said,
“I’ll pull the bottom end down with the pry bar and you check it with the
torque wrench." Wonder if he was "feeling" the bolt stretch or just from his
past experience was able to tighten up the main bearing caps and rod bolts
without me ever doing more than verify they were all in excess of the torque
since I didn’t get them to budge! I did put the heads on using the wrench
and the proper torque sequence per the articles I read.
Everything but the carburetor was now
together in the basement. Had not considered how much more it would weight
then when the parts were brought down separately!
Put it on a two wheeled hand cart. Took several friends with a rope
pulling and a few pushing and lifting to get the engine up the basement
stairs and out the door!
The flathead was easy to take out of the
Ford with a chain block and tackle. However this Olds was much heavier.
Could tell when we tired to lift it. Even the garage roof beam was
bending and we had to nail some 2X6 boards together to make a temporary
column to brace it! I had purchased some Olds-to-Ford motor
mounts. As mentioned with the engine parts I purchased was a flat plate adapter to
connect the stock Ford trans to the Olds. There was a pilot bearing adapter that pressed into the flywheel and
extended the hole for the transmission shaft to make up for the 3/8 inch
thick adapter. Another friend lent me a Ford transmission input shaft so I could bolt up the clutch.
Used the clutch that was in the Merc engine. His brother had built a ’28 Ford and offered to move my steering box into the
frame to clear the starter. He had an oxyacetylene cutting and gas
welding outfit. But I elected to buy what was called a "starter
switchover
kit" that moved the starter from the left to right side so it would not
interfere with the steering. It was an
expensive purchase and when I received it I realized I had to cut off a part
of the starter nose to clear the housing. I recall pondering how I would
get this done. Probably kept me up one night! I put a new blade on the hacksaw and started. Boy that
graphite in cast iron sure makes it easy to cut. Made the cut in no time!!
Photo right shows in red about where I had to cut the cast iron starter
nose.
We raised the engine and pushed the car
under it. We lowered the engine, and lowered it and kept on lowering it!
Boy was it heavy. Thought I had raked the car. It was several inches lower
in the front than with the flathead! I also recall those motor mounts didn’t fit
the Ford rubber donuts holes very well.
Had to file the motor mount holes quite a bit to get the bolts onto the rubber donuts.
Finally it all fit.
The left side exhaust manifold was
hitting the steering column! The solution was to use another
right had manifold which I picked up at the junk yard. I remember
struggling getting the nuts off and the fellow who was in the yard
to cut up parts put his cutting torch on the bolt and as I cringed he said, "Don’t worry it
won’t cut the cast iron." He proceeded to cut off the offending nuts
and the manifold was unscathed.
Pop's body shop friend welded the exhaust pipe pieces I fabricated and
hammered together to fit.
When I put the hydraulic lifters
together I had put a small amount of oil in each but as I cranked it over
none of the rockers moved. It took some time to get the pressure up and the
valves start to actuate. Put the valve covers on and hoped I had set the
distributor properly and the timing was good enough to at least start it
up. Even then it was known that you should run a new engine in for a ½ hour
or so. That I did and it ran fine! Set the timing with one of the week
lights we had at the time. I recall another friend having built an engine
and burned it out on his first run with no oil pressure. I loosened
the oil sender and saw oil squirt out! All seamed fine.
Had a local auto electrical wizard help get
the generator to work. He had to "polarized" it by shorting a terminal
to ground. Worked fine after that. However when the engine was
hot it cranked very slow. Fortunately a local company making
batteries, mostly for trucks, had what they called a 6-12 and 12-24 system.
The 6-12 was a two 6 volt batteries built into one case that had a solenoid
switch on top. It put the two batteries in series for starting and
then switched them to a parallel connection. All accessories, lights
etc were connected to an "always 6 volt" location but it put 12 volts on the
starter making it spin great. Just couldn’t run the starter too
long but with the increased speed the car started very quickly.
Had a local radiator shop block
off one of the inlet and outlets since the flathead had two of each. The car
would overheat and when I asked the radiator shop what they could do he had me
install a thermostat which I had elected not to use. As he explained;
"Your cavitating at the center of the water pump. Your boiling before
the radiator gets to 212 degrees!" He was right, it was a big help. No overheating except
at highway speeds. Went back and he made it a 15 psi pressure system. I
recall, he pressurized the radiator and found any leaky places and brazed
them. It worked. Used a 15 psi cap and let the temperature increase. For
all but sustained highway driving in the summer, which I did very little, it
was fine.
The car was really fast. However the skinny 16
inch diameter rear tires had little traction. When 1st gear
striped soon after the Olds was installed there was no problem. Taking off
in second could spin the tires until you backed off the gas! Also, to have
the gas peddle clear the higher Olds engine I had a piece brazed onto the
throttle shaft coming up at the firewall. It made the peddle have a
very short movement. Easy to get the wheels spinning. Drove the
car with two gears. The 4:11 rear and the torque of the Olds were more
than enough. One friend would bet, and mostly win, that he could beat a car on foot from telephone pole
to telephone pole from a standing start. I won that one easily. My buddy
with the '54 Pontiac sedan was very upset that I jumped several car lengths
on him in the quarter and left him in the dust! We had installed 3 X
2's on that car, it was light and quick but not a match for the '41! Even beat a few
motorcycles!